Tackling Toxics: How partnerships produced success at Founder’s Choice

Tackling Toxics: How partnerships produced success at Founder’s Choice

Founder’s Choice Cabinets, a manufacturer based in Tacoma, wanted to do something to help the environment as well as improve their business practices. By turning to Ecology, it not only reduced its environmental impact, but achieved stellar cost savings as well.

Founder’s Choice — a family-owned company that manufactures a variety of custom kitchen and bath cabinetry, and miscellaneous decorative and functional accessories — was looking to expand its cabinet portfolio and had experienced manufacturing challenges such as increased production lead-time. In an effort to improve operational performance and reduce costs, the facility reached out to the Tacoma-Pierce County Economic Development Board, who in turn brought in the state’s manufacturing extension partner, Impact Washington, and Ecology’s Lean/Green program.

Lean/Green is a customized service offered to Washington manufacturers in which continuous improvement principles and environmental methods are applied to help decrease operating costs and reduce environmental and energy impacts.

This public-private partnership received $100,000 from the State Job Skills Program and $25,000 from Lean/Green. The process improvements focused on:

  • Manufacturing efficiency training for staff.
  • Identifying and purchasing more effective equipment.
  • Recycling and reuse of certain materials.
  • Improved air compressor use.
  • Installation of LED lighting.
  • Methods to help improve and refine the manufacturing process.

Even as the company continued to expand its cabinet lines while adopting these process changes, the associated operational cost savings increased, while the dangerous waste, VOC air emissions, and energy use decreased (specific activity improvements and the projected results are shown in the table below). Founder’s Choice is now implementing recommendations and are on track to achieve:

  • $112,000 in annual cost savings.
  • 7,000 pound annual reduction in hazardous waste generated.
  • 20% reduction in Volatile Organic Compounds (VOC) air emissions.

We're looking for projects in 2021

Ecology and Impact Washington are looking for businesses interested in 2021 projects. To find out more about these grant opportunities, please contact:

Hugh O’Neill
hugh.oneill@ecy.wa.gov 
360-407-6354

Improvement activities

Process Category

Process

Estimated Reductions

Finishing Process Improvements

Spray can icon

Paint Spray Efficiency training for 5 staffs through the Pacific Northwest Pollution Prevention Resource Center.

  • Reduced short- and long-term staff exposure to VOC emissions

  • Minimized paint material usage by 15%

  • Reduced environmental liabilities

Purchase and install plural component spray guns to mix paint and catalyst at the point of application.

  • Reduced paint material usage and paint waste generated by 20%

  • Achieve annual waste management cost savings of $46,000

  • Reduction cleanup time by 10%

  • Improved paint job accuracy and significant reduction of on-job mistakes

Waste Management

Waste drum icon

Purchase and install gaskets for a solvent still to minimize vaporization of the recycled solvent.

  • Improved solvent recycling efficiency by 30%

  • Reduced solvent VOC emissions

  • Minimized amount of solvent still bottoms (sludge) disposed of

Flush catalyzed paint material in designated waste drums and recycling corresponding breakthrough solvent for reuse.

  • Reduced solvent waste generated by 50%

  • Significant reduction in labor time associated with catalyzed paint flushing

Energy Efficiency

Light bulb icon

Switch fixed-speed air compressor to variable frequency drive compressors to enable precise control of the speed of the motors that drive the compressor.

  • Significant cost reduction in energy usage

  • Reduced wear of the air compressor system

  • Increased power factor of the air compressor

Implement LED lights in finishing area.

  • Significant cost reduction in electricity consumption

  • Reduced output of defective cabinet parts

Product Work Flow Optimization

Factory icon

Implementation of automated track conveyor to conveniently transport painted and stained cabinet parts.

  • Reduced drying time of primed cabinet parts by 70%

  • Reduced staff travel and movement

  • Improved ergonomics

Development of individual paint and stain drying segment for the finished cabinet parts.

  • Significant reduction in staff wait time

  • Improved annual cabinet throughput